Quick disclaimer: This post may or may not be extremely long and saturated with photographs. I do not apologize, as the purpose of this post was both for chronicling Sam's surgery and for educational purposes of those who are contemplating a tear down of their own.Okay, as many know I have had a cooling system issue/chronic backfiring issue for quite some time. Most of the components of the cooling system were replaced or repaired at one point or another prior to the major surgery she was about to undergo.
After being
anesthetized and preparing properly courtesy of Rovers North, I went in with tools!
Pre-ordered was the head gasket, the intake manifold gasket, the valve cover gasket, the
carb rebuild kit, the swivel ball sealer and all the other miscellaneous gaskets and nuts and bolts necessary for completion.
First I took a long hard look at the engine compartment and made a mental list on what was going to be removed for work purposes only, what would be removed for cleansing purposes
only, and then what pieces would be pulled for cleansing, prime and paint purposes. Once the list was complete I started removing things. First thing was to drain the coolant, and then parts began coming off.
Battery, heater pipes, distributor cap, thermostat and housing, disconnect all the cooling hoses, remove spark plugs, valve cover,
carb, manifold, head ... for the most part in that order. Once all of the major players were taken off I did remove some extra things like the expansion tanks, the washer fluid reservoir, accelerator linkage, stuff like that to clean and paint.

Carbon residue on backside of carb ... right at #4 cylinder

Carb removed
Carb is off, juiced up head bolts, valve train is next followed by the manifold.
The valve train assembly took a little ingenuity from those guys at
Solihull ... the Green Bible outlines a method of removing the entire valve train without giving it an opportunity to fall apart on you, thus requiring an entire rebuild ... if you can find all of the bits you dropped! Basically once the retaining bolts are removed and the assembly is just resting in its location on the head, you take the valve cover you have already removed, flip it upside down and set it back on the train so that the retaining bolt holes align. Then you take the retaining bolts, thread them in enough to get good grip, and then pull the assembly off and the train remains intact.

Neat valve train removal trick ... the cover is upside down on top of the valve train.
I used the original valve cover bolts, threaded them back through just enough
to get tension, and then lifted the entire assembly out of the head.
The head gasket, when removed, did not look nearly as bad as I had thought/hoped. All of the cylinders looked fine, #4 was a little charred but that's where I figured my problem was to begin with so I was okay with that.

Head out of the truck, old gasket in foreground.

Head removed, uncleaned.
I scraped the gasket off, cleaned up the face and prepared for new installation. I checked the plane and all looked good, so I installed the new gasket, all nice and shiny, and then proceeded with putting the head back together.
New head gasket in place. Shiny compared to the old one I scraped off!All went on smoothly, everything looked good. There was a big amount of carbon build up on the backside near #4, so still, right along.

Cylinder #4 ... this is the end I felt I was having problems with. As I uncovered
things, it all pointed to this end of the gasket.
All the planes looked decent, so I put the finishing touches on some of the painted pieces, reinstalled, and then set about putting the rest back in place. Before installing the valve cover I re-
gapped all of the tappets as they were all misaligned.

Valve cover gasket in place.
I started with the thermostat housing and ran into my first problem. There are three bolts holding it into place, and the third I went to tighten down was going fine until finally it broke free - snapping itself off in the housing. While this may sound horrible, it was actually the best bolt to snap as the hole goes all the way through; the other two seat into the head, so I lucked out. A quick trip to Lowe's for some grade 8 bolts and I was back in business.
Put all the housing back together and then made short work of the remaining bits, aside from the accelerator linkage which gave me some trouble, but then all was good. I started filling her up with coolant in hopes of a successful first-fire and noticed coolant ... lots of it oozing out of the gaskets around the thermostat housing. The manual didn't call for any
RTV so I hadn't used any ... drain coolant
from drain bolt, drop bolt while draining, search feverishly for bolt beneath me with thumb plugging the hole ... find bolt, install on second time, get up soaked with anti-freeze and disgruntled.
I changed clothes, becoming a little more irritated all along. Back to work, remove thermostat housing, coat in
RTV on both sides,
re tighten all of the coolant hoses, bolt back together.
Reinstalled the
carb, as I had already rebuilt it the previous night. Read the removal instructions in reverse from the Green Bible to ensure I hadn't forgotten anything stupid and all looked good.
I sat in the driver seat a little anxious ... I knew the fuel bowl in the
carb would need to fill before she fired up so I gave the key a turn and let her try and crank; and then she did, and fired up right away. She sounded like she was running high, so I tinkered with the
carb until she was running right. A quick test drive around the block
was successful for a few minutes ... and then she died on a turn. Just shut down.
After a few minutes of fiddling with her in the dark I phoned a friend who towed me home. Once I got her under the lights I found the culprit ... the ignition wire running from the coil to the distributor had gotten tangled in the accelerator mechanism when I put it back together. After putting a new lead on, and zip tying it into place, she started right up.

Much cleaner and nicer looking than before.
A drank a beer and celebrated the moment.
Conclusion:
With proper planning and no unexpected surprises this was a job that could have taken four to five hours, from tear down to all systems go. It took me closer to 12 overall because A) I did the tear down over the course of a week B) I cleaned and painted a lot of things I didn't have to C) I did a valve tune and
carb tun and rebuild and D) I broke a bolt off in the thermostat housing and had to burn time going for parts. I rounded the day out with removing a lot of the previous owner's wire-
tying handi-work ... there were lots of green and yellow zip ties in the engine compartment which just didn't seem right so I removed them all started from scratch with black.
Definitely scores a 3
out of 5 on the difficulty level, mainly because there is no
real skill necessary, but being able to read the manual is extremely important. The directions are step by step and it is simply a matter of taking enough things off the engine to get to the gaskets that
need replacing.
All in all though, a great educational experience and a fun time with Sam! Even baby girl got to help!

Emaline honking the horn and scaring the crap out of me!

Me and my girl after a long day's work.